New Landing Gear
I have been patiently waiting for my new Aluminum Landing gear from Grove Aircraft in San Diego. My friends Mike and Neal Lafrance actually own the hanger next to Grove.. Even with that kind of pull, I still have to wait 8 weeks for the gear. As Robbie explained it to me, its out of his hands because the gear has to go to a heat treat shop 3 times during its construction. I have 3 more weeks to wait!!! I decided that the simplest way to add a landing gear to the Prototype was to attach it to the outside of the fuselage in the same location of the old one. I needed to add some additional bearing blocks and increase the area of the two diagonal stiffeners . Truth be told, I should have done that for the original gear.My goal is to have all of the modifications done and the Fuselage recovered by the time I get the gear. I want to be able to just bolt it in and then flip the plane over.
reinforced gear frame |
in this picture the extra doubler on the two diagonal members are shown. all of the vertical loading of the gear is reacted by these members. They also need to react the aft braking load by a heel and toe reaction between the gear fitting bolt and the back wall of the fitting. underneath the plywood is 1.5" of birch plywood bearing blocks. .
outer landing gear fitting |
This picture shows the outboard fitting for the new landing gear attach fitting. There will be a narrower fitting that is bolted to the inside of the gear frame. Both plates will be welded to a .125 plate that will act as a bearing plate. I will have two 3/8" bolts permanently brazed to the 1/8" plate. I will counter bore into the birch doubler to clear the bolt head. Sitting on top of the plates will be a radius block. The gear will be sandwiched between two of these radius plates. The isead here is to limit the gear bending moment to the gear itsself. The radius blocks will act like two fulcrums.
Unfortunatly this new gear will add 8 lbs to the Robin and may put the prototype out of the part 103 category. I'm sure with the redesigned wing and the single cylinder 2 stroke engine, Part 103 will still be possible. After my talk on Labor Day, the universal opinion of everyone I talked to was to scrap the 2 stroke and Part 103. My Friend Murry Rozansky who is the ESA Treasurer, suggested that I look at the 23hp Briggs and Stratton Vanguard conversions. After some research, I have decided that this is the perfect engine to adopt. The Prototype is actually perfect for it from a weight and balance point of view. My CG will move forward to 22% at full fuel. 26% empty. The static margin increases by 10%. This engine will be far more reliable than the 2 stroke. I will however fly this plane on the MZ 34.
2 comments:
Hi Mark,
Just a weird random thought..
..could a landing gear spring be made from a 1985-mid1995 GMC Safari/Astro fiberglass leafspring?
Theoretically I guess it could, but the configuration is all wrong
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