Test set up with members of the "Brain Trust" |
Test set up showing nose angle |
The wing panel itself was mounted inverted with the nose angled downward at 14 degrees. This is to simulate the abrupt pull up condition at the max maneuvering speed. This will induce the leading edge compression load that will verify the leading edge spar and the fitting.
The actual load was 90 lb bags of ready mix concrete. Fortunately a neighbor was just starting a fence project and was gracious enough to let me “borrow” them for a day. The load schedule was designed to emulate the constant loading of a rectangular “Hershey bar” wing with the parabolic drop off that occurs near the tip. The bags were to be placed in 1”g” increments. The design criteria I established was to have no skin wrinkling less than 2.5 “g” because I am trying to maintain laminar flow. After the first “g” of load was placed, it was realized that this wing would have too much deflection. It was decided to continue the testing to see where the weak link was in the design.
At appox. 3.5 “g” the deflection was 21 inches at the tip . When we attempted to add the next “g” load, it was noticed that there was severe web buckling between the main shear pins. This area of the wing used a box spar with a 1 inch foam core. The bond had failed obviously between the main web and the foam. A complete shear failure occurred shortly after the buckling was noticed and the wing broke.
Shear web failure caused by web instability |
Investigation of the foam bond joint revealed that there was never a complete bond to begin with. I built this portion of the spar on a very hot day and due to the insulating properties of the foam, the epoxy and micro balloon mixture had an exothermic reaction and never bonded to the web. I realized that this could easily happed to any builder so I immediately revised my design to eliminate the foam box design and use bonded vertical stiffeners instead. I found a product used in the electric motor business called NEMA grade C fiberglass insulation. This is a fiberglass sheet product made from 120 style glass and polyimide epoxy resin.. Its produced in an autoclave and is rated to 450 degrees working temp. Besides being a high quality laminate and product, its also cheap and available in numerous thicknesses. I was using ¼” thick plates as the main intercostals at the shear pins. I used .063” thick plates for the vertical stiffeners.
I decided to retest the wing to verify the new stiffeners and to verify the shear capability of the root web. The wing spar shear web lay up schedule is constant out to wing station 36, because of this I cut off the damaged inboard section of the spar and rebuilt the outboard 18 inches of the spar by adding a new shear pin intercostal. The outboard section of the wing was damaged when the spar struck the ground so that portion was cut off and discarded. I bonded a wooden plate to the outboard section of the undamaged spar so that I could gain enough leverage to emulate the design bending moment at the new “root” It was decided to test the spar in the up right position. Load was applied with a floor jack through a load cell I designed. The cell consisted of a hydraulic piston with exactly one square inch of area. Automatic transmission oil was pressurized and the pressure read by a hydraulic pressure gauge. The readout was one for one. The cell was calibrated at a local truck weigh station.
Testing verified that the shear web was fully stable at the design ultimate load of 1325 lbs. The final design of the prototype wing incorporated bonded vertical stiffeners and roughly double the amount of graphite used in the test spar.
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